Chapter 6 - Fabrication Method for WFSRD
Devices
6.1 - Introduction
As noted in Figure 5.21, the device parameters chosen for fabrication are:
- NS1 = 1017 cm-3
- NS2 = 1017 cm-3
- NB = 1.5 x 1014 cm-3, p-type
- λ = 30.6 μm
- L = 150 μm
- A = 1.35 mm2
Unfortunately each one of these values falls outside the normal ranges of values typically
encountered in a VLSI fab. The surface dopings are quite low. Usually, one wants them to be as high as possible to
ensure a good ohmic contact. As for NB, lightly-doped p-type substrates are generally harder to obtain
than lightly-doped n-type substrates. The value of λ given is very, very long compared
to normal VLSI standards for diffusion. (Values on the order of 0.1 μm are more common).
Lastly, the thickness L is quite thin, compared to standard wafer thicknesses.
6.2 - General Approach
Three general methods were considered for fabrication. The first approach consisted of thinning a
standard wafer with a background doping of NB down to the desired device length of 150
μm, and diffusing in the remaining dopants. The primary disadvantages of this approach were that
the thin wafer might complicate handling and yield, and that the high value of λ would
require a very long time in a very hot diffusion furnace (approximately 10 days at 1250 °C). The advantages were that the thinning process was relatively inexpensive (US$110/wafer), and the diffusion
could be done in-house with existing equipment at Carleton.
The second possible approach was the use of variable-dopant epitaxy to grow the exact profile
desired on a thick conducting substrate. However, this would require a relatively thick (but not unheard of)
epitaxial growth. Also, obtaining reasonable control of doping at 1014 cm-3 levels would
require a large amount of experimentation. For these reasons, quotes for performing this growth commercially (at
Lawrence Semiconductor Research Laboratory, Inc.) proved to be expensive (US$2750 setup, plus $175/wafer). The
possibility of performing this epitaxy in-house on Carleton's AET RX rapid thermal CVD system existed, however, at
the time this thesis began, this equipment was brand new and not yet operational, and represented relatively
untried technology.
Both of these approaches yield essentially one-dimensional structures. More complex schemes,
involving selectively thinning a thick substrate were also considered. However, endpoint detection in thinning
etches would be problematic. Also, the increased dimensionality is undesirable, as it would likely introduce
undesired parasitic effects.
For these reasons, the first approach (thinning and long diffusion) was chosen.
6.3 - Substrate Preparation and Dopant Implantation
By happy coincidence, wafers with almost precisely the desired value of NB were
available from a surplus-wafer broker. Furthermore, these wafers were float-zone refined rather than
Czochralski-refined, which is highly desirable for high-voltage devices. Float-zone material tends to produce
devices with higher breakdown voltages, due to lower oxygen and other impurity content [Ghan83]. (The Czochralski
refining process is performed in a quartz crucible, which leaches some oxygen into the molten silicon. Float-zone
refining isolates the molten portion of the silicon ingot from contact with any crucible.)
The complete wafer specifications were as follows: Prime Grade, <100>, Boron-doped,
75-95 Ω-cm, float zone, 4 inch diameter, two standard flats, polysilicon backside,
510-540 μm thickness, made by Wacker-Siltronic, US$14. Twenty-five wafers were
purchased.
To thin the wafer to the required 150 μm thickness, fifteen wafers were
sent to Virginia Semiconductor for chemi-mechanical polishing (CMP). Only eight wafers survived the process, due to
the thinness. The others shattered. Upon their return, the eight wafers were cleaned in Caro's acid (1 litre of
sulfuric acid at 100 C, mixed with 100 mL of 30% H2O2) for ten minutes, and rinsed in
de-ionized water.
At this point, six wafers (designated "A" to "F") were sent to Implant Center Inc, to implant the
remaining dopants. A dose of 2.7 x 1014 cm-2 of boron was implanted with a moderate energy of
80 keV on one side of each wafer, and a similar dose of phosphorus on the opposite side. The dose, Q, is related to
NS and through the relationship:
(6.1)
For NS = 1017 cm-3 and λ = 30.6 m,
Qimpl = 2.7 x 1014 cm-2. The total cost was very low, approximately US$130. One
wafer ("B") broke during implantation, due to the wafer's thinness.
After the wafers were returned from implantation, one wafer (designated "A") was cleaned in
Caro's acid. Apparently due to thermal shock, the wafer broke into two roughly equal-size pieces. However, as it
had been the intention to break the wafer into several pieces at a slightly later stage, this breakage did not
present a significant problem and processing continued with this wafer.
6.4 - Dopant Drive-In Diffusion
The dopants introduced by the implants were redistributed to obtain the desired values of
NS1, NS2, and λ by using a drive-in diffusion. However, as noted
earlier, the large value of requires a very long and hot diffusion. Simulations on the Suprem III simulator
indicated that to obtain the desired values, a drive-in time of approximately 180 hours was required if a
temperature of 1250 °C was used. (This temperature represented the maximum usable
temperature of the quartz tubes that were available.) This long diffusion raises two potential problems: that of
dopant suck-out, and impurity diffusion. Dopant suck-out occurs when the dopants evaporate out of the silicon
wafer, or diffuse into the surface film. Impurity diffusion occurs when temperatures are high enough that
impurities (like sodium) can diffuse through the furnace quartz tube and enter the wafer.
The first problem was addressed by adding an oxide layer on the wafer "A" to seal in the dopants.
The "LOTOX" (low-temperature oxide) was added by placing the "A" wafer in the furnace in an oxygen atmosphere at
405 °C for 15 minutes. Judging from the gold color of the deposited oxide, the oxide
thickness was about 0.2 μm. Suprem III simulations indicated that this would be sufficient
to contain most of the dopants. (A standard pre-furnace RCA clean was performed before the LOTOX
deposition.)
After the Lotox deposition, the wafer "A" was broken into ten smaller, roughly equal-size pieces
designated "A0" to "A9". These pieces were cleaned in a standard HCl-H2O2 mixture (chosen so
as not to etch the protective oxide), followed by a brief 5% HF dip. Pieces "A1" to "A9" were then placed into the
furnace for the drive-in. The furnace operated at 1250 °C, with a 2% oxygen, 98% nitrogen
atmosphere. (The nitrogen was chosen since it is relatively inert, and the oxygen prevented any nitride formation
on the wafer surface). At twenty-two hours intervals, approximately, the wafer pieces were removed from the
furnace, and the furnace tube was gettered with HCl for one hour, at 1250 °C. After each
gettering, one wafer piece was removed, and the remainder were reloaded into the furnace. In this manner, pieces
with drive-in times of approximately 23 hr, 44 hr, 65 hr, 86 hr, 107 hr, 128 hr, 149 hr, 170hr, and 199 hr were
obtained, corresponding to A1 to A9, respectively. This was done in order to calibrate the drive-in process,
relative to the SUPREM simulations. This process took about 10 working days. On weekends, the wafer boat was moved
to the end of the furnace tube, and the temperature was dropped to 1000 °C, with a
nitrogen purge. This effectively halted the drive-in, on weekends. (This measure was taken as a precaution against
power outages, or other equipment problems which might arise over the weekend, when technicians were not
present.)
Wafer pieces "A5" to "A9" were sent to Solecon Laboratories Inc. for spreading resistance
measurements, so that the doping profiles could be examined. The results of these measurements are shown in Figure
6.1, in doping-concentration form rather than in raw resistance measurements. (The resistance-to-doping calculation
was performed by Solecon.)
Figure 6.1 indicates that both A8 and A9 have nearly the ideal doping profile. The only
significant deviation is the 30% lower-than-expected surface concentrations. Evidently, some dopant evaporated, or
was "sucked-out" into the oxide layers. This should not have a significant impact on device operation, since the
active region is the lightly-doped area around the junction. (However, relatively poor forward-bias conduction can
be expected, due to poor ohmic contacts.)

Figure 6.1 - Doping profile as a function of
drive-in time.
As a result of the drive-in, approximately 0.7 μm of oxide coated the
wafer pieces. This was removed by etching the wafers in a 10% HF solution for approximately 35 minutes. (The
endpoint of an oxide etch can be determined by observing when the silicon surface becomes
hydrophobic.)
6.5 - Lifetime Killers
At this point, the fabrication sequence branched into two parts. One portion of wafer A.8
proceeded directly to metallization. A second portion, redesignated "A8.PT.850", had lifetime-killers (platinum)
introduced, and then proceeded to metallization.
The platinum impurity centers were introduced into A8.PT.850 by dipping the wafer into undiluted
Emulsitone Platinumfilm, a spin-on dopant source. The wafer then underwent a four hour, 850 °C, oxygen atmosphere diffusion to drive-in the platinum. Surface oxide was removed with a 10% HF
solution.
6.6 - Metallization
Both A.8 and A8.PT.850 followed the same metallization steps.
The silicon surfaces were cleaned with a 2 minute, 900 V, 100 W sputter etch in 8 milliTorr of
argon, to remove any oxide that had grown during the time since the HF etch, or indeed any other surface
contamination. All sputtering was performed using a Materials Research Corporation 8620 diffusion-pumped
multi-target system.
A chromium target was pre-sputtered by a 3 minute, 1.25 kV, 100 W etch in 8 milliTorr of argon.
The wafer piece was then sputtered with the chromium for 20 minutes, at the 1.35 kV, 100 W, 8 milliTorr argon
settings. Identical pre-sputtering and sputtering steps were then performed with a gold target. This produced a
6000 Å thick gold layer, bonded to the silicon surface with a 1000 Å thick chromium adhesive layer. The
silicon piece was then flipped, and the process repeated, so that identical metallization existed on both sides of
the wafer.
Gold was used as the top metal to ensure that the diode could be easily hand-soldered
to.
A photomask was generated on a 2.5" 2.5" glass substrate (designated CU-170-01). The pattern
consisted of 45 mil 45 mil squares (representing the desired metallization) on a 50 mil grid (1 mil 25 m). A
positive photoresist (HPR-504) was applied to one side of the wafer, and was developed. The exposed metallization
was removed with a 60 minute, 900 V, 100 W, 8 milliTorr argon sputter etch. The excess photoresist was then removed
using acetone and Microstrip 2001. It was found that a black residue (presumably charred photoresist) remained on
the metal surface despite the use of the photoresist strippers. This was removed with the gentle use of a cotton
swab.
A dry etch, rather than a wet etch, was used to remove the excess metallization in the belief
that a dry etch would introduce fewer contaminants, such as potassium, which might have deleterious effects on the
breakdown voltage.
To reduce sputtering damage, and to improve the metallization adhesion, the wafer underwent a 15
second, 450 °C rapid thermal anneal (RTA).
A Tempress diamond scriber was used to scribe "A8" and "A8.PT.850" into individual devices
(designated "A8.n" and "A8.PT.850.n", respectively, where n is a number). These devices where
then separated by running a roller over the wafer surface, cleaving the devices along the scribe lines.
